[T2] Sat and the bus in Baltimore

[T2] Sat and the bus in Baltimore

accessys at smart.net accessys at smart.net
Mon Dec 7 13:45:49 MST 2015


ok fuel presure holds steady at 34psi
removed 3/4 injectors checked spray pattern
hyd lifhters set 1.5 turns in 
timing set at 7.5BTDC

distributor was built backwards so #1 is at 10oclock (has been like that 
for years and we did double check it.) when we put in spare dist gap was 
set to spec, (can't remember but looked it up) and wires were reconfigured 
to #1 at 4 oclock
is
T4
crane high output ignition (but we tried it with a stock unit)
hyd valves
trigger wire on term 1

all other wires were compared to running bus backed up to mine and in same 
places
double checked operation of double relay
checked fuel pump operation and presure

engine has run which is worst part.

Bob



On Mon, 7 Dec 2015, Jamie wrote:

> Date: Mon, 7 Dec 2015 14:38:44 -0500
> From: Jamie <jrivers at globalserve.net>
> To: accessys at smart.net, type2 at type2.com
> Subject: Re: [T2] Sat and the bus in Baltimore
> 
> Bob, when are you going to offer up some facts.. like fuel pressure?
> reset valves... I have to assume you did it correct.. I can't pick up on what 
> you did wrong.
> checked fuel delivery.... wtf does that mean... 1 psi and 100ml per minute is 
> way too low..
> set timing to what ??
>
> sort of like the MATH teacher always says... show the work so we can see 
> where you went wrong
>
> you really need to create a signature and update with the facts ,, like 1978 
> ,T4, 2L , EFi , crane ignition, 28psi fuel pressure, solid valves set to 
> 4thou gap, dist #1 wire on cap at 4o'clock, wires CCW 1234... ECU trigger 
> wire on coil term 1,
>
> "only sound we got was a backfire"
>
> this makes me think... big vac leak... timing way off.... both,,
>
>
>
>
>
> ----- Original Message ----- From: <accessys at smart.net>
>> 
>> so Sat Dan Besson comes up and he has a very similar bus to mine even down 
>> to the Crane ignition.  so for over 6hrs we did.
>> pretty much everything but included
>> 
>> reset valves
>> checked fuel delivery
>> replaced plugs and wires
>> replaced Dist witht stock one with points
>> swapped parts between engines
>> stuff that worked on his wouldn't work on mine, stuff on mine workedh on 
>> his.
>> set timing many times
>> cranked while turning dist
>> checked every wire and hose
>> replaced S boot
>> fixed a wire on cold start relay(not a no start factor, just noticed it)
>> and cranked and cranked and cranked and only sound we got was a backfire 
>> from ether when timing was off.
>> a neighbor even wandered by and asked if it was going to run again as he 
>> watched me a couple months ago when it ran the one time (oh and it was 
>> stopped and started several times during that run)
>> 
>> I really appreciated Dan coming by but when he left at sundown we were no 
>> further along then when we started...
>> 
>> Dan thanks again for trying to diagnose this thing
>




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